Ended up getting my parts early. FCP Euro is handy since they ship from Milford, CT. Even the free shipping is like 1 day, or it was this time. Crazy.
Anyway this job was easy and exactly what I had planned for. Of course I am accustomed to the trans situation so no stress this time. That was nice. Maybe 2-3 hours or something, taking my time. You could probably do this in like 45 minutes on a lift if you were in a rush but rushing transmission stuff doesn't seem like a good idea. This was the first time I've ever had a valve body out of a transmission and it wasn't difficult.
Order of operations:
Drive on ramps, jack up by diff to level or slightly higher for more room. Remove rear two bolts from center bottom cover and 4 bolts from the rear cover, remove rear cover. Drain trans fluid. Remove 6 pan bolts. Lower pan and sort of drain and just use care to avoid spilling what's left in the pan. Disconnect electrical connector, unscrew adapter sleeve, pull sleeve out of trans. Remove trans filter, set aside since I was reusing. Remove 10 bolts (same size as trans pan, T-30) and lower valve body carefully. It is heavier than I expected. May be steel instead of aluminum.
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Laid out some bubble wrap as a cushion and liquid barrier and then 2 layers of my blue shop towels. I brought the valve body to my bench and took those pictures.
Changing the solenoid was easy. Remove 1 bolt that holds the bottom 2 solenoids (in the picture in the last post). Simply pull the TCC solenoid out and push the new one in. Reinstall the hold down bracket and bolt. I made it tight. I tried to clean some of the trans fluid off of the valve body and conductor plate. Not sure that was really necessary but I felt like it. Used some brake clean, shop towels and air.
I did check the resistance of the old and new solenoid. They were basically identical, around 2.86 ohms. Spec is 2-4 ohms from the diagram above. But electrical health does not have anything to do with mechanical health (it is a moving part).
Installing the valve body was a little tricky. Mainly it was the weight. Once again, would have been easier on a lift. You have to align some things but mainly ensure the shift selector is centered on the pin. I knew to watch for that (didn't want a repeat of no gears, though for a different reason). Anyway I finally got two bolts started and got that going. Torqued to 8Nm....hope that was right.
Snap filter back on. Clean pan out again and reinstall that. I torqued those bolts to 8Nm also. I cleaned out the connector with electrical cleaner and compressed air.
Anyway it all went back together with no issues.
It ended up taking almost 4L by the time I topped it off hot. So I guess another 50% of the fluid has been changed. It must be at like 85% fresh fluid at this point.
As for the road test, I did not get to test it cold but I can say this: I still feel a difference in TCC lockup performance. It seems way smoother and properly integrated with the actual shifting, as they originally intended. I am actually feeling confident that I fixed the cold issue but I'll have to wait until tomorrow to confirm that. Even still, there are some notable differences in the way it drives and shifts. This is a PWM TCC clutch and, like my STS, it is intended to slip much of the time. Well, now it seems to be slipping the proper amount. This also helps drivability both because RPMs are a little higher (more torque) and because the NVH jerk has been smoothed out when applying throttle. I actually caught it hanging at 2000rpm once when I tipped in when rolling. This is because the TCC initially was slipping and then gently engaging. Again, this is as intended I am sure and feels way better.
I'll report back on the next cold start. Hopefully it's fixed or significantly reduced!